Where you at vintageblueoval you get the problem figured out? are you on the road again?
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the saying"Guns kill people" is like saying that pencils misspell words............MY BIO66' coupe been setting for 10 years, 289 c code with auto trans.85000 miles on engine and I am the third owner. needs quarters,doors,fenders,tank,interior,and a 1000 other little things I am sure,but I love her!
I Now have a 67 C code Fastback that needs more than the coupe. Still plugging away on the coupe feverishly so that I can get to the FB
Well you drove 60 miles without a problem, so its time to stop replacing parts.
Sounds like a head gasket is allowing combustion gasses into the cooling system creating an air block, old car very simple cooling system.
new waterpump radiator,t-stat,fan good idea checking the spring on hose.
your at the point where you are second guessing yourself, take a breath and take time diagnosing the problem. I wish I was near you I would be out to give you a hand. good luck
Last edited by DRAGPAK428; 11-23-2009 at 09:02 AM.
So Im back home in Atlanta, finally! That old 65 fought me every step of the way, and it still has a LONG way to go. I got the cooling problem fixed last week in California. I had to pull the heads and found several of the water passages completely clogged in the heads. I pulled the freeze plugs and blasted out those passages with the hose. It seemed like a few pounds of junk came out of there! Once it was all back together after a 13 hour thrash, the car ran fine, nice and cool.
I drove it to Vegas, over the Cajon Pass with no issues. Then it was on to the Grand Canyon on Friday morning. Once I arrived in Winslow, AZ the car started running rough and missing at idle. I quickly suspected it was vaccum related and was correct when I found the vaccuum advance in the distributor not working. The closest place I could find a replacement distributor in stock was an Autozone in Flagstaff so we pressed on to the Canyon and took her easy on the way to Flagstaff. Grand Canyon was AWESOME by the way! The car started missing pretty badly on the grade up to Flagstaff but kept on running. Once we were off the highway, it stalled on the way into the Autozone parking lot and we coasted into a parking space. I grabbed the new single point distributor, installed it in about 5 minutes and it fired right up. I adjusted the timing and she ran great!
Now it was back on the road, hoping for Albuquerque before gettting a good nights sleep. The car was running better than ever, all the way through Gallup, NM. As we approached Grants, NM I started to hear a light ticking. It was only happening at steady cruising speed and my mind first thought of a misadjusted valve. It quickly got louder over the course of 5 or so miles. I pulled off at the next exit. Completely forgetting my engine is a 77 302, I pulled the valve cover, expecting to find a valve that needed adjusting. No such luck. The metallic particles in the engine oil was pretty telling about the real cause. I figured I would try to get into town at Grants, NM so I got back on the highway for that 5 or so mile stretch, hoping to find a motel or something for the night (it was about 11pm and 20 something degrees out)
3 miles down the road came the clatter and knock of a bottom end coming apart. I coasted off the next offramp and into a nowheresville gas station and thats where my old Mustangs road trip ended.
A 2am tow truck ride into Albuquerque was next (115 miles away). We caught a ride to the airport, rented a Kia Rio and limped the Mustang into the Park & Ride lot for airport travelers. We finished the trip back to Atlanta in that little Rio. At least it got 38 MPG.
Now I gotta get back to Albuquerque and get my car. It looks like I'm gonna take my F150 and flat-bed trailer out there this weekend and pick it up. I'll get my camera downloaded and share some action shots of the repairs and the first legs of the trip. I should have them up in the next couple days. I'll also keep updating the thread as I get the engine apart (again) to see what really happened.
So that definitely sucked. But it was still a good time, albeit an expensive one! I have no idea what caused that bottom end to come apart, the engine has a legitimate 45,000 original miles. Anyway, not a huge deal to repair or replace it. I just wasn't gonna go for it on my back in a Motel 6 parking lot when its 30 degrees out.
You know maybe 45,000 was just all she wrote on the '77 small block. After all, I bet they didn't drug test in the engine factory back then and there was a little of that [drug use] going around.
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The stable:
65 'T' Coupe 302 HO 5 speed (5/65) ~ First Mustang
65 'A' Convertible 4 speed Factory GT (5/65)
65 'A' Fastback 289 4 speed (2/65) ~ Calico driver
65 'A' Coupe 289 Auto Factory GT (3/65) ~ Parts car
66 F100 460 Auto ~ Grandpa's truck
Here are some pictures from the day I pulled it out of the barn. It hadn't moved in 5 years, hasn't been driven since early 2000. Funny, all the things I had worried about... brakes, suspension, carb, electrical stuff... all worked perfectly. Who'da guessed?
Here she is with the heads off and this is a cool shot from the South rim of the Grand Canyon. If any of you are thinking about a Grand Canyon visit, do it! Spectacular!!
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